My dad was down in Phoenix for a week, so I put him to work helping me get the
motor finished up and running. Actually, he was doing a lot more than helping me -
he pretty much had all of the knowledge and know-how (not to mention a big box
of parts), and I was just sort of the wrench-fetcher. My dad had aquired a
Rochester Quadrajet carb off of a 1972 Blazer and it looked to be in great shape,
so that was one of the first items we tackled.
The distributor was an HEI unit out of a 1977 Chevy 1/2 Ton pickup. My dad had
tested it before he sent it down, and it had a good strong spark. Most of
the old wires were in good shape, so we just used those for this test.
The water pump and alternator were already installed, so we put on the belt and
that was done. We also installed a new mechanical fuel pump and bent up a
custom metal fuel line to the carburetor.
We mounted the radiator and then had the not-very-fun task of finding the correct
radiator hoses. On our first attempt, the bottom hose we got ended up being the
right length and shape, but didnt fit the water pump outlet correctly. We didnt
know what upper hose would work, so had to settle for a flexible hose. However,
the flexible hose also didnt fit over the thermostat housing correctly. We had to
make a return trip to Napa, where the parts guys let up go upstairs and just browse
all of their hoses. We found two that seemed like they would work, and when we
returned home to try them out, both were a perfect fit. (For reference, the upper
hose is Napa part number 7884, and the lower is 7651).
I re-used the stock Toyota oil pressure sending unit and temperature sending unit.
The temperature sending unit screwed right in with a small adapter, but the oil
pressure sending unit took a little bit of creative use of fittings to get things
to connect up properly. I also installed the electric fan control module into the
head, although we didnt hook up the rest of the wiring for this test (we just wired
up the fan directly to a switch).
Finally, we wired up my stock instrument cluster so we could keep an eye on oil
pressure and engine temperature. We also wired in some standard house AC switches
to simulate the ignition (one to fire the starter, and one to the distributor so
we could kill the power). There wasnt a fuse anywhere in the whole mess. Not probably
the typical way of doing things, but it ended up working out really well for this test.
After finding out that no Napa or Checker stores in all of Phoenix had an oil
pump priming tool for sale or rent, I finally found one at an Autozone. However,
when we went to use it, something wasnt right. The tool wouldnt catch on the oil
pump and kept slipping. We took it out and compared it to the distributor and
found that the tooth that engages the gear was too large to fit into the groove.
Frustrated, we finally ended up disassembling the tool and grinding down the flange,
then putting the tool all back together. After our modification, it worked flawlessly.
As we spun up the drill, the oil pressure gauge began to rise. Once we knew we had
pressure, we put the distributor back on for the final time. We roughly set the
timing using top dead center and then it was the moment of truth.
We hit the switch to turn on power to the distributor. Then I hit the switch to fire
the starter. It cranked and cranked, but wouldnt fire. After much deliberation, we
determined that the carb wasnt getting any fuel. We checked a few fittings and fixed
the problem. Time to try again. This time, we hit the switch, and the motor fired
and started! I had been waiting for that moment for almost a year and a half! My
dad quickly dialed in the timing and the engine was running great. It sounds
incredible and we only had one small leak that simply required tightening a hose clamp.
I was very excited to finally have an engine that ran. However, the joy was short-lived.
After making a few adjustments, when we tried to fire it up again - nothing. The engine
wouldnt fire. Argh! We determined that there was no spark. The distributor that was working
so well and just had plenty of spark a few minutes earlier was no longer working. It was
getting late and I was frustrated, so we called it a night and tackled it again in the morning.
The next morning, we did a few tests to try to isolate the problem. We figured it was either
the coil, capacitor, or electronic module in the distributor. In order to avoid driving back
and forth to the parts store all day, we just bought all three parts (my dad is going to put
an HEI in his landcruiser soon, so any extra parts would not go to waste). We changed them
out, one-by-one, so we could see what the root of the problem was. First the coil - reassemble
and...nothing. Then the capacitor and terminal...nothing. Finally, we replaced the electronics
module and put it all back together. I had bad thoughts of it still not starting, but I
crossed my fingers anyway. I flicked the switch and the engine fired up - what a huge relief!
# posted by brian dunnington @ 2/01/2006 09:07:00 AM